H
huntb
Guest
When I first got the bike it wouldn't run without the choke on. I pulled the carbs and cleaned them up and got them back in. The first thing I noticed is that it wouldn't start right away. I would start it and it would sound like it was trying to start but would just die out. Then all it would do is crank unless I let is sit for several hours. After trying that about 4 or 5 times it finally started and ran without the choke but it is idling at 4k.
I shut it down and backed out the idle adjustment screw completely (counterclockwise right?) but it didn't do anything. The intake boots were replaced within the last two months by the previous owner but tonight I will try checking the screws to make sure they are tight and spray WD-40 around them to check for o-ring leaks. I looked at the throttle cable this morning before I left for work and it doesn't look like that is the issue but I will verify again tonight. Also, the choke is not stuck either.
Two things:
- After I assembled the carbs I drilled out the pilot screw plugs, tightened them and then backed them out 2.5 turns. I don't see this being a problem but maybe is is?
- The air box boots have shrunk and do not fit well over carbs 2 and 3 so there is definitely some freer flowing air going into at least those two carbs. I just ordered a replacement box today off eBay.
Has anyone had experience with this or know what might be causing it? Any advice would be appreciated
I shut it down and backed out the idle adjustment screw completely (counterclockwise right?) but it didn't do anything. The intake boots were replaced within the last two months by the previous owner but tonight I will try checking the screws to make sure they are tight and spray WD-40 around them to check for o-ring leaks. I looked at the throttle cable this morning before I left for work and it doesn't look like that is the issue but I will verify again tonight. Also, the choke is not stuck either.
Two things:
- After I assembled the carbs I drilled out the pilot screw plugs, tightened them and then backed them out 2.5 turns. I don't see this being a problem but maybe is is?
- The air box boots have shrunk and do not fit well over carbs 2 and 3 so there is definitely some freer flowing air going into at least those two carbs. I just ordered a replacement box today off eBay.
Has anyone had experience with this or know what might be causing it? Any advice would be appreciated