Should I have walked away..probably...time will tell.
Once I got it home things got worst;
Carbs not fitted correctly to airbox.
Oil leak underneath engine
oil leak from camcover -I'd spotted that and knew I'd be checking valves anyway.
Electrics a complete mess - poor connections/earths
Back brake seized - pedal only.
Choke linking bar bent,so chokes wouldn't completely close and 1 of the grub screws missing ,stopping no1 choke from coming on at all .
Jet sizes bigger than standard on 3 carbs (102.5) and 1 at 100 !
Air filter disintergated and airbox leaking. Breather hose not connected.
Today I decided to replace the clutch rod oil seal,which appears to be the source of the oil leak,but had to remove the front sprocket ,which was almost new and found that the spocket nut was loose and was been retained by the locking washer. Once I bent back the locking tabs the nut "fell off" ..........completely stripped ! At least the drive shaft thread seems to be ok and all the damage is on the nut thread.Who would fit a new chain and sprockets knowing they had left it like this ?!!!!!!!!!!!!!
I also started working on the carbs and found the mixure screws were only 1 1/2 turns out and according to spec,should be 3 1/2 turns out.
If anyone's interested I'll update this as I progress....or not.
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