here is a pic shared via google https://photos.app.goo.gl/ZGYDHrFwemQBGgpB8
here is a video https://photos.app.goo.gl/CDt3CUCmoEBs9RF37
am I doingt something wrong here? It took me a while to figure out how to get the other one out but once I got it in the right place it came out pretty easy but I am stumped on this one and don't understand why it's not working.
The other exhaust valve (the one got the shim out off) was over spec, I think the measurement was .107 and spec is .04-.08 while this one is super super tight, is this normal? I would think they would all be similar or at-least out of spec tight over loose? I think I read here somewhere that exhaust valves tighten up over time?
Here is my history with the bike. I bought it in 2017. It developed an oil leak from the base gasket so I decided to have the engine rebuilt by a friend who was started a shop specializing in vintage bikes. Ran it stock and it ran amazing for years. I rode it all over the country 4 times. Got stolen in 2020 recovered in 2021 pretty trashed (there's a thread about it here somewhere) The thief put pod filters on it and I decided to go with it (perhaps a mistake) so I had a different friend who is great with vintage Japanese carbs rejet the bike and with minimal work I ripped around town on it for a couple months. It developed some other issues so I decided to take it off the road and considering my busy life I don't have as much time to wrench as I'd like so I'm slowly going through it trying to make it a reliable around town bike for fun commuting.
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