Took the bike to the track, had a great day, bike was running really great, until I lost a oil cooler hose, the engine oil spilled onto the track, and my engine, and my rear tire, and I went down.
rebuilt the bike, started it up, heard a weird noise on the left side of the engine while trying to get it timed, but it disappeared on it's own. checked behind the alternator cover. nothing amiss.
once the bike was ready to ride for a shakedown, I was hearing a sound that sounded a lot like brake pad/rotor drag, but it was coming from the left side of the engine. kind of like a sliding sound... weird. engine ran fine, but the sound was there and it was RPM dependent.
rode it to work yesterday and got downtown and saw that the crankcase breather was puffing smoke heavily. this happened in winter 2017, I had to put a top end on it then. engine still ran fine, started easily, idled ok without having to adjust any settings from track day. got it home, didn't run it hard.
compression test results tell the tale:
1 -120
2 - 80
3 - 105
4 - 110
got the boroscope out and shot some video from inside the cylinders. i'll post a YouTube video of that in a little while. piston 2 crown has some damage for sure.
for now, i'm looking at parts.
probably an 1134 kit, +2mm pistons (about 6-700)
slotted cams because why not ((about 120)
will check integrity on rocker pads
put new valve springs in last rebuilt (gsxr springs as recommended by the shop)
hopefully valves and seats look okay
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