I had some trouble getting the carbs tuned just right last December when I finished her up. Got directed to Koolaid Kid's idle mixture adjusting procedure and performed that as directed.
My pilot screws were set at 2 turns out, and that turned out to be way to small. After the procedure they ended up at 2+3/4 turns out and the bike ran greater than ever. Pulled hard right off of idle and dropped back down to idle quickly and stayed there. Perfect.
So... I put the bike up at the end of December after doing that final tuning. Fuel stabilizer in the tank.
Just got her out of storage this past weekend since the weather was nice. So, what's the problem?
She runs like crap now!
The symptoms are that any attempt to roll on throttle from idle is met with an immediate bog, and a big one. Bike just about dies. The only way to stop the off-idle bog is to leave the choke partially on. (Yes, the bike is completely warmed up during this testing.)
That's the same symptom that I had before doing the idle mixture adjust procedure which resulted in a 2+3/4 turns out setting on the pilot screws and a great running bike.
It sounded like a too rich condition, so I reset the screws to 2+1/2 turns out to see if it made any difference. A little, but I still have the big off-idle bog.
What the heck happened over the two month storage period? What could have possibly changed when the bike was running perfectly back in December?
Can't be fuel starvation, since the bike runs fine at speed once it gets up there. Just doesn't have any off-idle power at all.
HELP!!! Any advice would be appreciated.
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