The issues I now face now are a light smoke rising from the cam cover. Not sure about the origin though. Doesn't smell like gas or oil (at least strongly like them). I did the valve adjustment, and I think there may have been some oil splatter from trying to depress the tappets. Alternatively, perhaps it is from the new Real gaskets warming up to the new operation? I ran the bike for a solid 10 min after wardmup..
The second issue is revving above 2k (thought I don't trust my aftermarket tach...). I have not taken her out on the road just yet, but she cuts power at around 2k rpm/half throttle. Yes, I looked here-
I did some very minor damage to the pilot jet on #2 (and left it) during the rebuild, but that isn't even the same throttle band as the pilot jet affects.
I would just like to mention how incredible an effect the valve adjustment and carb rebuild had on how the machine runs! I will testify to the benefits of doing this maintenance! Despite it not running "perfectly", she is so incredibly smooth and inviting... Hopefully taking her out tomorrow, hopefully addressing the issues tomorrow too!
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