it takes a small shot of carbcleaner and im off and running
if I pull the choke out it revs ok and all cylinders heat up in about a minute
then it begins to go all over the map for rpms up to 5000 and then pretty much stays there
I have put kits in the carbs so new jets, pilot jets, idle screws, blew them out twice
was not sure if the idle mixture screws go spring, washer, o ring??
Clymer does not a show a pic of that screw
left carb idle screw is stuck but could live with that if the rest works for the other three its at two turns now anyways
There was one CV spring that was smaller than the other three is that the problem? are they sposed to be all the same I have extras?
I ran the bike directly off a bottle of gas and same issue
I have inspected the boots they look new and there is no change even if I loosen the hose clamps and rock the carbs and spray wd40 or use propane to look for leaks.
compression is 120 120 130 150
new plugs new dyna coil packs new wires new ignition new airbox new filter new number two carb vacuum hose
ran the engine with the airbox off just to see that all CVs play together
Carefully Bench synced the butterfly valves set the floats to 21 mm
If the head were cracked wouldn't the compression even be worse?
Not making any oil so it seems floats are good ones ..I shook em during the overhaul
left it on prime one night no gas rushing out so assuming new needle and seats working good.
after warmup no cleaner needed fires right up and is a runaway
I could check each carb by loosening the float drains
I set the Idle mixture Screws at 2 turns out tried 2 n a half to one n a half guess what still running away on me
It dogs out of power when I tried to go around the block
So far not even one foot traveled
there is NO rust in the fuel system I sucked open the vacuum line and got great flow and the new line is clear so if it ever leaks id see it.
I bought a petcock diaphragm but the off tank test yielded no difference yet
It makes no difference if the throttle or choke cables are even connected
all positions are as low as they go as is the idle speed setting
Anybody know what is wrong??
Way big thank you if I get back on the road
Ps the airbox is back on and till my filter arrives I have simulated it with a brand new sponge don't laugh to hard
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