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    #16
    Ok second notch made it worse

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      #17
      Well, thats leaning it out so two options from here. Go down one notch from stock to richen or, as suggested, raise the float height. Let us know how it goes.
      1982 GS550M Rebuilt Winter '12 - 550 to 673cc engine conversion.
      1989 Kawasaki ZX-7 Ninja
      2016 Ducati Scrambler Full Throttle

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        #18
        I just posted this, but here goes again.



        Start with the mains. The DJ138's are fat and should be fine for a stock 1100E with pods/pipe. You are having problems off idle. That should NOT be a main problem, it COULD be a needle problem, but that is what the DJ needle is for. The 47.5 pilot is the standard setting for 1100E pods/pipe DJ kit so you are good there. You are only left with idle circuit.

        Have you done the basics like sync crabs, set idle mixture, vacuum leak? Carbs on and sealed? The issue should be idle circuit stuff.

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          #19
          Originally posted by posplayr View Post
          I just posted this, but here goes again.



          Start with the mains. The DJ138's are fat and should be fine for a stock 1100E with pods/pipe. You are having problems off idle. That should NOT be a main problem, it COULD be a needle problem, but that is what the DJ needle is for. The 47.5 pilot is the standard setting for 1100E pods/pipe DJ kit so you are good there. You are only left with idle circuit.

          Have you done the basics like sync crabs, set idle mixture, vacuum leak? Carbs on and sealed? The issue should be idle circuit stuff.
          +1, I had assumed you had done the mains already.
          http://img.photobucket.com/albums/v5...tatesMap-1.jpg

          Life is too short to ride an L.

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            #20
            Originally posted by niclpnut View Post
            If it's pulling 3-4k to redline 3/4 and wot the float height adjustment should help on that needle transition just before.

            My fzr 1000 was doing the same thing. Raised the float hight 1.5mm and pulls like a train.

            Just readjust the mixture screws once your happy with he float height. Probably won't need them turned out quite so far.

            Nic
            Yes forgot about float height

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              #21
              Originally posted by posplayr View Post
              I just posted this, but here goes again.



              Start with the mains. The DJ138's are fat and should be fine for a stock 1100E with pods/pipe. You are having problems off idle. That should NOT be a main problem, it COULD be a needle problem, but that is what the DJ needle is for. The 47.5 pilot is the standard setting for 1100E pods/pipe DJ kit so you are good there. You are only left with idle circuit.

              Have you done the basics like sync crabs, set idle mixture, vacuum leak? Carbs on and sealed? The issue should be idle circuit stuff.

              Carbs are synced, going to pull it all off today and start over.

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                #22
                I appear to have bigger issues, head is coming off

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                  #23
                  Oh no, what happened?
                  http://img.photobucket.com/albums/v5...tatesMap-1.jpg

                  Life is too short to ride an L.

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                    #24
                    Originally posted by jwhelan65 View Post
                    I appear to have bigger issues, head is coming off
                    Sorry to hear about it, but good time for an 1166 and some head work.

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                      #25
                      How much run time is on the engine?

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                        #26
                        Originally posted by GSX1000E View Post
                        How much run time is on the engine?
                        Roughly 30k

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                          #27
                          Originally posted by tkent02 View Post
                          Oh no, what happened?
                          Brand new plugs are gooey black

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                            #28
                            Originally posted by posplayr View Post
                            Sorry to hear about it, but good time for an 1166 and some head work.
                            Early 82 with original crank, a bit hesitant to take on the 1166 kit. Starting fresh on the head for sure...
                            Last edited by Guest; 03-17-2014, 06:35 AM.

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                              #29
                              So what are you suspecting as "Bigger Issues" ?
                              1984 GS1100GK newest addition to the heard
                              80 GS 1000gt- most favorite ride love this bike
                              1978 GS1000E- Known as "RoadKill" , Finished :D
                              83 gs750ed- first new purchase
                              85 EX500- vintage track weapon
                              1958Ducati 98 Tourismo
                              “Remember When in doubt use full throttle, It may not improve the situation ,but it will end the suspense ,
                              If it isn't going to make it faster or safer it isn't worth doing

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                                #30
                                Originally posted by hjfisk View Post
                                So what are you suspecting as "Bigger Issues" ?
                                I have oil puking out the exhaust ports around the header.

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