Where in at right now:
Air filter and air cleaner box lid were gone when I got the bike. Filter was replaced with a 4" round paper element. Original was a foam element.
Stock jetting was 42.5 pilot 110 main. Bike would idle great, but surge and hunt at steady state low throttle cruise.
Went to a 47.5 pilot and 112.5 mains. Surge was gone, running super rich on low throttle, wouldn't run past 6k WOT.
Went back to 110 mains and 47.5 max revs increased to 7k, still rich on cruise.
Went back to stock pilot, 112.5 mains, lean cruise, revs still stuck.
Now 42.5 pilots (stock), 120ish mains (drilled, flow checked against the 112.5 to make sure they were flowing more, because at first they weren't because I neglected the entry and exit radii, and balanced with the other drilled jets) lean cruise, will rev to 7k and then very very slowly pull higher.
All grounds checked, coils grounds redone, coil signal and ground wires position swapped, new plug wires. I've tried running with the "choke" on, with and w/o the air box lid, with and without the filters, nothing seems to be getting me even close. Want to beat my face against broken glass.
Does it sound like it needs more or fuel up top or less?
Still haven't tried going with a smaller main.
Next thing I'm going to try is wrapping the filter in an old t-shirt.
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