-Carbs stripped and dipped.
-New orings on carbs and rubber plugs on bottom of pilot jet hole
-New intake boots on engine
-New boots on air box
-Factory air box sealed and new foam air filter.
-Valves adjusted
- New spark plugs
- Coil relay mod
- Carbs synched and mixture screws set to 1.5 turns out
- Pilot jet 40 and Main jet 92.5
I am running factory pipes and air box. Nothing is changed from stock. I have checked spark and have sufficient spark on all cylinders. I have verified that the float level is correct with the float level tool. Plug does not look oil fouled it is fuel fouled for sure (dry black soot). I have switched the plug wires from 1-4 and #1 still fouls out. Tonight i leaned the mixture screw out on #1 1/4 turn and took it for a short ride around town. I pulled the plug out when i got home and it was already all black and sooty. Should i lean the mixture screw more and see what happens? How far can i turn it in before tearing anything up? I think it has something to do with the pilot circuit because i mostly just ride around town at 1/4-1/2 throttle all the time. Should i try a hotter spark plug? Im just not sure what my next step should be.....
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