Here's a quick run down of what I'm working with:
- Freshly Rebuilt Carbs
- Dynajet Stage 3 Kit (170 Main Jet)
- K&N Highflow Pods
- 4 to 1 Exhaust (Dented)
Ever since I rebirthed him, he's had hesitation issues. At first I thought it was the jet needle height, so I raised 'em to the second to last notch. Not much better. Installed the K&N's hoping it was a lack of air issue. No better.
A few months have passed since the original shake down and I took her for a test ride today.
Here's the updated symptoms:
- #4 carb spits back into it's pod pretty frequently, particularly on deceleration.
- Acceleration is smooth, steady until about 1/2 throttle.
- At 1/2-3/4 throttle he lurches, intermittently losing power.
- If I try to open from half to full, power plummets. Seems to be starved of either air or fuel.
I checked the plugs yesterday and they were pretty white. This, and he's hotter that he should be makes me think that he's running lean. I also mentioned above that the 4 to 1 has a pretty good sized dent from the PO bottoming out. I'm wondering if it's causing intake/exhaust issues...
What do my symptoms point towards? I'm thinking that tomorrow I'll raise the jet needle up to the last notch and do a dynamic sync of the carbs (currently only bench synced). With the pipes as they are, I can imagine that the syncing is pretty far off.
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I should note that I'm waiting on a tach cable currently, so I don't have any way to read RPMs.
Thanks for any insight.
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