I don't have too many pictures from unmounting everything, so I have to use a bit of text here. Later pictures will help understand what's going on though.
All bolts came out without fuss. The nut used on the #2 collar was very loose, and not putting any force on the collar. The only reason I didn't vibrate off is because it's a nylon locknut.
After sucessfully removing the exhaust, I found the bolt hole around the stud you see in above image almost completely gone. The stud was hanging on to only a few threads of a helicoil in there, whose existance I only discovered later on. The stud could be easily moved sideways by hand, with obscene play. So I removed it carefully.
When I put everything back on, I used new stainless bolts, and torqued them to spec, erring on the lower end of the specification (methinks it was around 1-1.6 kg⋅m), making sure that the threads matched up good. When it came to the the bad hole, I made sure the new bolt did find thread, and began to carefully screw it in, only by finger force at first, and then using a small wrench lightly.
Snap.
Helicoil disintegrated:
State of the hole:
Needless to say, I was frustrated beyond any measure at this point.
How the hell does one f$!ck up an exhaust bolt hole this badly? How much of a kludge must one be? I wished the responsible PO's bloodline to dry out, and other non-printable cussing.
Timeout.
Comparing the used stud to a regular bolt:
gave me the idea that the helicoil was further in to begin with, and that the shorter bolt only grabbed to an exposed part of the helicoil. So I tried to reuse the stud, but no dice.
Well, the good thing is that the re-drilled hole doesn't seem to penetrate all the way into the block.
After calming down enough and getting over my frustration, I fastened the collar enough with the remaining bolt in order to be able to get home:
It worked, I got only very minor blow-by. I think. At this point it was cold, dark outside and I just wanted to get home, get my mind off things.
You'll notice that I reused the fat spacer PO used on the stud. Reason was that I found the bolt hitting spec torque way before holding the collar. That could be either due to the now slanted position of the collar, or that the factory drilled the holes on #2 badly. I'm leaning towards the latter, it would also give some explanation to PO's screw-up.
After pondering this for a while now and winning a bit of motivation back, I think I getting a time-sert in there, with something "lock-tite-ey" (not sure what would stand up to the heat there) could be a viable option. Welding would be better, but as far as I understand welding aluminium is very challenging.
Other than that, I can't think of anything else short of disassembling the engine and swapping the head. But as far as I understand, that's a delicate operation, I have never done it before, and I don't think I'm properly equipped.
Your thoughts?
Comment