1981 GS550T, all stock except for a K&N in the airbox. When I got it it ran not so good
-Shimmed the valves
-New o-rings in all four carbs. Totally disassembled, dipped, etc.
-New intake boots and o-rings
-New plugs
-Changed the oil
After all of that, it was running quite well. It seemed lean, but nothing dangerous. With this newfound confidence I decided to try out a Kerker 4-1 I acquired awhile back before I even had a GS. Install went fine, and it even ran pretty good, but broke up a little bit in the mid range. Instead of just putting the stock pipes back on, I decided I was going to try jetting up a hair for this new exhaust. I thought it might even be the answer to it running lean on the stock pipes. When I had the carbs apart previously I noted that it had all stock jetting, despite a PO previously stating that it was jetted. So 92.5 in the mains, and 40 for the pilots.
I drove all over Texas trying to find 97.5/100 mains, and 42.5 pilots. I finally found the last of them this afternoon, and came home to put everything together. Put the carbs on the bench, installed new 97.5 main jets and 42.5 pilots, double checked the float height, and everything seemed to be in order. Put the carbs back on the bike, got it fired up, let it warm up awhile, set the idle mixture with a colortune, and decided she was ready for a road test.
That's where it all went to crap. Idle was fine, any throttle at all made it break up like mad. WOT with the choke pulled was somewhat decent. Got it up in the revs, killed it, pulled the plugs and it appears to be WAY lean, which seems very counterintuitive having added a decent amount of fuel to the equation.
Tomorrow I'm putting it all back to stock except for the pilots, one of the stock 40s was broken, so I don't have a full set to go back in.
Can any of you think of something I might be totally overlooking?
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