A few weeks back, I synced the carbs (bench first, then carbtune). I got them dialed in just right (2&3 even, with 1&4 just a little higher), and right around the middle of the scale. It was idling beautifully, had it dialed in around 1000 rpm, and throttle response was great. When I took it for a spin, I noticed some mild popping when letting off the throttle, figured I just needed to tweak the mixture. But when I got it home, I came to a stop and it stalled out. If I dialed up the idle, the rpm was way too high next time I started it. One of my air boots (#1) felt a little loose, so I ordered a full set. New boots are tight.
I re-synced the carbs again this weekend. This time, the vacuum pressure was low - off the scale (I believe <8 cm), so I had to flip the carbtune to get them synced. I finally got it so the bars were synced up, but they were all just above the bottom of the "right side up" scale. During both these tests I had the petcock vacuum line plugged. After all this, I tried adjusting the air screws again and settled around 3 turns out.
Took it out for a ride this morning (about 30 minutes), and it repeated the same behavior: sporadic popping when letting off throttle, then towards the end of the ride, it stalled out whenever I would let off the gas long enough for the idle to drop. I again tried dialing the idle adjustment screw so it would hold an idle, though when I would blip the throttle, the rpm wouldn't drop off quickly, but would "hang" for a bit. After letting it cool down for a few minutes, when I started it up the idle was up >3K. I pulled the plugs, and #s 1 and 4 were white, though I'm not sure if that's from the last ride or my previous attempt. So I'm guessing that I still have air leaks, but despite multiple attempts at spraying all around the intakes, I haven't found any.
I'll try dialing the air screws out a little farther, but if they're already at 3, I don't think I have much more room to play with. Is there anything obvious I could have overlooked?
Here's the long list of what I've done:
- Adjusted valves, replaced gaskets
- Fully stripped and cleaned carbs following both sets of instructions on Bikecliff's site (multiple times), including checking all passages
- Replaced o-rings & float gaskets
- Adjusted floats (by measurement, not yet set up to directly measure fuel levels)
- Replaced air filter (Uni filter and oil)
- Re-sealed airbox with weatherstripping
- Replaced airbox boots and carb manifold pipes (along with their o-rings)
- Tested for leaks around intake boots a couple times (sprayed with wd40 and carb cleaner)
- Replaced all fuel and air lines
- Synced carbs with Carbtune Pro
- Adjusted pilot screws, starting at 2.5 turns (all currently around 3 turns)
- Oil, filter
- New battery
- New NGK plugs (PO had recently replaced leads, also NGK)
- Cleaned tank (EvapoRust)
- Recent petcock (replaced by PO, looks new)
- Tested compression (on a cold test, all 4 are within spec, haven't tried a hot test)
(Also, FWIW, exhaust is stock, though I have a rattle in the right side pipe so I know there's some internal rust. But no obvious external rust or holes. I haven't tried replacing the exhaust seals yet, though there are no obvious signs of leaks.)
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