Ran like crap and would hardly start.
I finally got it to idle by going 6 turns out, but the screws were about to fall out, but at least it would run. I double checked that I was thinking it was lean by putting my hand over the airbox hole, and it sped up. Ok, that means it's lean.
Next problem was that it wouldn't accept 1/4-3/8 throttle.
I picked up some 50 pilots. I wanted 47.5 but they only had three. I also read an old post about some 1100 owners all raising their needle to the 5th clip. I turned the screw in to 2 out (from 6 out) to start with.
1.5 was the best. Now the bike ROCKS! I probably would have been at 4 turns out with the 47.5s. and throttle response is killer everywhere with raising the needle to the 5th down.
I am going to ride it for a while to get a better feel for any dead spots, then do a plug reading at several throttle openings. Then I'll use my free dyno run coupon that came with the DJ kit.
In summary:
Stock airbox, K&N filter, lid in place, stock motor, V&H 4-1 Street Megaphone
Main jet: DJ114
Needle: DJ 5th clip down from top.
Pilot jet: 50
Mixture screw: 1.5 turns out.
-Kevin
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