It has a stock 4 - 2 exhaust & a "Uni" foam filter.
It ran well at Bruce's (5000 feet & hot) without the filter or side covers on the box but seemed to have a flat spot on lesser throttle positions although I didn't run it for long.
On the way back it seemed to come to life in Sacramento when we got under 2,000 feet & cooler temps.
Here at sea level it runs much better but is still surgy at WOT & gas mileage is not that good (max 40mpg on a run, generally 30-35mpg)
The carbs were cleaned just before I bought it & here's what it says on the receipt:
Replace main jet to 122.5
Drill slide to close faster
Mixture screws 3 turns out
Needle move up 2 steps (from this I guess it has a Dynojet kit fitted otherwise there shouldn't be any steps.....)
Last time I pulled the plugs they seemed ok to me, possibly a little rich but I'd just been running around town & parked it, I did nothing special beforehand.
I haven't done any chop tests yet.
I haven't opened up the carbs yet to see what is actually in there.
I'll try it with no filter here up & down the street sometime soon & open the carbs up for a look at what's there. (Never opened these before but I've messed with some webbers)
It seems to me that if I go back to stock mains & move the needle back down it will probably be somewhere close.
I guess I'll need to buy or borrow a set of synch gauges too.
My other option is to get a K&N in box or pods & 4-1 pipe to lean it out that way. The pipe is on it's way out anyway but I do have the option of buying another stock set (but maybe I'll sell those & go 4-1 anyway.....)
Dan
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