Since January, this bike has had a new wiring harness installed to replace the one that melted the main fuse. Along with the wiring harness came a new fuse box, new r/r, both handle bar switches. Had bike working for about a week, before I noticed that this still didn't correct my charging issues so the stator was then replaced along with the battery to a AGM battery from bikebatts.com. Had bike running for about 2 weeks when the starter clutch went. I then had the starter clutch and rotor replaced as the issue was sheared bolts through the clutch into the rotor. I also at one point installed a fuel filter.
I now have the bike back, but am having issues with the bike running. It started out as an occasional stutter or bog down while riding. It would clear and take off again like nothing happened. Yesterday I ran close to a hundred miles with out any incident after once on start up after sitting for an hour. This morning I rode to work, again no issues in the forty-five minute ride. I went out at lunch and maybe 500 yards out of the parking lot, it started bogging down. I could not get the bike over 2K rpm, if it went over 2K while going down hill, it starts bucking and backfiring. Using the choke(enrichment) circuit makes no difference. I have been running some sea foam though the bike more or less constant since I got this bike in November, that is at least when it would run.
After limping home I checked for air leaks using carb cleaner, non seemed to be evident. I then pulled the air filter out of the bike, this, too, seemed to make no difference.
Please any suggestions on where to look would be greatly appreciated.
Thanks,
Dirk
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