You'll have problems....
So last fall I had a cold pipe on #4 after idling, spark was there so I assumed a stuck float , needle or something due to improper storage. I wanted to take a look at the carbs anyway since they'd been on for a couple of years and I needed to replace the mains with 122.5s since they had (I'm pretty sure) 117.5s in them.
Bottom line, I pulled the carbs and swapped out the mains. I checked the needle jets while I was in there and everything was pristine, not even sediment in the bowls.
Carbs are now back in, all boots in good condition, clamps tight, fuel in every bowl, good spark, slide in #4 carb moves freely, the rubber skirt is OK and I can feel suction at the test port on the boot (I've got my Carbtune hooked up) but I'm still getting no heat out #4. 1,2&3 all sizzle the spit off of my finger but I can hold my finger on #4 pretty much as long as I want. Its warm but nowhere near hot.
I also "bench synched" the carbs according to the factory manual with the first little bitty bypass port showing and just the slightest hair of the second port. Thats what the drawing looks like so thats how I set them up.
Air jets (or whatever the real name is) are 1.25 turns out and I've tried up to 3 turns out.
I guess my next step is to bring home my compression tester from work and/or buy a leakdown tester.
Am I missing something, any ideas? What would you recheck first...
Thanks in advance.
/\/\acmatic
P.s. Yeah, I'm back. Life got a little hectic there but my new job allows me time to breath.
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