It was running great last year and the plugs were a perfect light brown cinnamon color with cheap emgo pods and a Kerker 4 into one.
After removing all the body panels I replaced the old emgo's with new emgo's but now she is running real lean.
Did I change the air flow by removing the side panels?
Last year I was running:
stock pilots
132 mains
needle shimmed up about 30 thousands
Now I have:
Stock pilots
190 mains
needle shimmed up 100 thousands
The bike runs strong and pulls hard down low but when I get on the express way and really lay into it the top end falls off like I have a rev limiter by the time I hit 4th gear WOT it will start to sputter cough and die.
If a deaccelerate and wait about 30 seconds or so let the clutch out while coasting it will fire right back up and run strong again.
Check the plugs and they are way lean!
I think I am sucking the float bowls dry?????????
I pulled the petcock off double checked everything screen and diaphragm every thing is clean and operating properly.
New gas and vaccum hoses on the carbs, no vaccum leaks, and the carbs have been throughly cleaned and synced.
It ran good last year and earlier this year just after removing the side panels and changing the pods it went real lean.
Has anyone ever come across anything like this am I missing something.
Sorry for the long post just trying to all the info out there
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