Main jet @ 135
Adjustable (not DJ needles, but adjustable) at 4th clip from the bottom
pilot 47.5 (started at 45, read that it was lean, tried one step up, and the following happened)
Float settings at 22.4mm
Screw settings Tried anything from 1/2 turn to 4 turns and...
Well after going over the Factory Pro step by step tuning guide i surmised that my pilot jets seemed to be one step too small at the stock setting. The screws had no effect over idle, and it seemed to surge as if lean thru 0-1/8 turn on the throttle, signifying to me that they were indeed lean, along with the popping on decel. Well, today i tried some freshly cleaned 47.5 pilots (45 is stock) and the bike was having no part of them. It simply would NOT idle. No matter the screw setting, if you took it off choke the bike would flutter and die. I removed the carbs and the boots were sopping wet with gas. Evidently it was simply flooding it out? But would a one step increase really cause this much of a problem? Dropped back to the 45s and it idles, but still acts lean.. Do i actually need to step down on the main and its drawing too much thru it? I dont think that is possible but im no carb genius either... Float levels too rich STILL?? anyone have any ideas? Help or info would be greatly greatly appreciated!
TCK
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