B
badbrown
Guest
After struggling with flat spot issues, weak spark, overconsumption of fuel, etc. I went ape and went through the entire bike again and fixed everything again. Now the bike is running better than ever. I guess the first go around fixes were'nt enough so here it is. Intake boots sealed. Airbox boots tight. All negatives cleaned grounded nicely. Replaced corroded connecters on battery, pos and neg. Reconfigured power source to DYNA S. Checked all voltage to coils w less than one volt drop loss from connecters. Reduced aomount of connecters to coils and Dyna. New Ignition swich (key switch) not kill. I opted to do these things instead of the coil mod which I feel is unneccesary at the moment.
So I have a 4-1 exhaust, Airbox with no lid. VM carbs with stock pilot #15. Needle on richest setting, and 102.5 mains. 2 turns out on air screws and float height 24mm(stock). Carbs synced and chop tested (currently).
So I have a 4-1 exhaust, Airbox with no lid. VM carbs with stock pilot #15. Needle on richest setting, and 102.5 mains. 2 turns out on air screws and float height 24mm(stock). Carbs synced and chop tested (currently).