B
bluewool
Guest
Hello, I am in the process of resurrecting my GS. The latest challenge has been the electrical system. The battery was not charging, I bypassed the rr check and went immediately to the stator output (no need to blame the toaster if the circuit breaker is off) 0vac at all rpm. Ω test revealed a dead short and two opens. I immediately started to make plans to rewind it myself seems pretty dead simple. However, after removing it I may not have to. I have seen the pictures and thought I'd up load the one of my particular failure because I haven't seen any other ones like it. The stator itself appears to be fine, (I'll bring my megger home tomorrow and check the insulation) but the connection of the harness to the stator coil shorted phase to phase. It is not uncommon for poorly soldered joints to fail over time. Hopefully the coils survived and I'll just replace the harness (it has hardened over time and the insulation seems like it could crack away) solder the connection, epoxy them and put it back in. While I'm at it I will DeOxit the connections for the rr and check it over. What really surprised me was the chintzy crimps they soldered over make the connection.