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Bogging at 3500 RPM & at a loss where to go next

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    Bogging at 3500 RPM & at a loss where to go next

    With your guys help I've made progress but not riding yet. I got the carbs cleaned....very clean. Like Pacman suggested I got the low speed passages in the carbs taken care of and that took care of the bogging I encountered as I gave it throttle.

    Now I can get it up to 3500 but then it bogs. If I give it choke (no throttle) I can get 4000-4500. Where to go next?

    '80 850L - New intake o-rings, new carb kits (stock), airbox is definitely sealed, K&N air filter recharged. It idles and warms up very nice. Backfires some on startup until it settles down after minute. I can't find any air leaks.

    Suggestions? Worked on this thing all last summer and still haven't gave up hope but would like to take one ride this year

    #2
    Also float heights are in range and float (tested.)

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      #3
      Valves adjusted and carb sync done?

      Comment


        #4
        Yes and yes

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          #5
          Throttle slides lifting correctly?
          Holes in diaphragms?
          Spark advance operating smoothly?

          Sounds like too lean when it is bogging, if the choke helps.
          http://img.photobucket.com/albums/v5...tatesMap-1.jpg

          Life is too short to ride an L.

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            #6
            Throttle slides seem to be correct and slide nicely.
            No holes in diaphragms that I could find, used a light to shine back through.
            Spark advance operating smoothly, how would do I go about checking that?

            I'll play around with the choke when it is bogging down and report my find this evening.

            How high should I be able to rev with just the choke?

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              #7
              Originally posted by Roemy24 View Post
              Spark advance operating smoothly, how would do I go about checking that?
              With a timing light.


              Were the installed jet(s) the correct size(s) as the originals?
              De-stinking Penelope http://thegsresources.com/_forum/sho...d.php?t=179245

              http://www.thegsresources.com/_forum...35#post1625535

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                #8
                One more thought: When I rebuild my carbs, the jet needles that came with the kits were tapered wrong (more blunt) than the originals and as a result, are still in the drawer.

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                  #9
                  Make sure the holes in throttle slides are stock size & haven't been enlarged by someone else....

                  Definitely check your needles. I would use Mikuni only. Did you renew the clamps for the carb boots & airbox? The K&N does flow more air than stock so that won't be helping. If the 850 is like the 1000G box the side plates have to be sealed properly to the box otherwise air can get in the side & bypass the filter.
                  1980 GS1000G - Sold
                  1978 GS1000E - Finished!
                  1980 GS550E - Fixed & given to a friend
                  1983 GS750ES Special - Sold
                  2009 KLR 650 - Sold - gone to TX!
                  1982 GS1100G - Rebuilt and finished. - Sold
                  2009 TE610 - Dual Sporting around dreaming of Dakar..... - FOR SALE!

                  www.parasiticsanalytics.com

                  TWINPOT BRAKE UPGRADE LINKY: http://www.thegsresources.com/_forum...e-on-78-Skunk/

                  Comment


                    #10
                    When I put the new kits in, I stayed with the original needles because I noticed the difference. All the jets where correct as the originals. To tell you the truth, two clamps just broke last night on me. I think I'm going to order new intake and airbox boots to help elminate some problems as well as clamps. As for the K&N, I know I have the sides sealed very well. Would I need to turn the air screws to compensate for it?

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                      #11
                      So some more evalution. No leaks around the intake boots. No leaks around the airbox boots however I get a slight rise (500rpm) or so when I spray the top of the side covers, both sides. Yes that is a problem but I can't see it would cause all this problem. I'll take care of that in the days to come.

                      I can rev it to 4500 and pull the choke and it will race to 5-6K then backfire a few times and practically die out. Is it time to pull the carbs and clean for the fourth time? The only issue I had this last time was the needle valve seat filter screen/filter kept falling off. The new ones don't stay as well as the originals. I would attempt to clean the originals but have seemed to miss place one and missing a screen from another. I did verify that they were on the best I could when I reassembled.

                      Also I was only able to get it to around 4K before so I backed out the air screws to almost three turns each. It did seem so run a little better and did get my RPM's a little higher.

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                        #12
                        partially cover the air snorkel opening with duct tape and see if it runs better, or temporarily duct tape around the chrome end caps and see if it runs better.

                        your air box has the rubber style end seals correct ?(I don't have a gl to look at)
                        if it does, glue the rubber seals to the air box, lightly put some grease on the air box seals and check for a complete impression of the side air box seals to end covers.
                        Last edited by rustybronco; 05-26-2009, 06:01 PM.
                        De-stinking Penelope http://thegsresources.com/_forum/sho...d.php?t=179245

                        http://www.thegsresources.com/_forum...35#post1625535

                        Comment


                          #13
                          Yes, those leaks could be causing your problems.

                          You also might want to think of getting a spacer stack (load of washers) from Radio shack & going up one spacer (stack of washers same height as the plastic washer - take one & put it below the clip allowing more of the needle to "poke through" at the top.
                          This is like raising the needles half a notch (if it had notches like the old days) & it might help a bit.
                          1980 GS1000G - Sold
                          1978 GS1000E - Finished!
                          1980 GS550E - Fixed & given to a friend
                          1983 GS750ES Special - Sold
                          2009 KLR 650 - Sold - gone to TX!
                          1982 GS1100G - Rebuilt and finished. - Sold
                          2009 TE610 - Dual Sporting around dreaming of Dakar..... - FOR SALE!

                          www.parasiticsanalytics.com

                          TWINPOT BRAKE UPGRADE LINKY: http://www.thegsresources.com/_forum...e-on-78-Skunk/

                          Comment


                            #14
                            If the carbs are clean and the airbox tight you may be looking at a weak ignition.
                            1983 GS 1100E w/ 1230 kit, .340 lift Web Cams, Ape heavy duty valve springs, 83 1100 head with 1.5mm oversized SS intake valves, 1150 crank, Vance and Hines 1150 SuperHub, Star Racing high volume oil pump gears, 36mm carebs Dynojet stage 3 jet kit, Posplayr's SSPB, Progressive rear shocks and fork springs, Dyna 2000, Dynatek green coils and Vance & Hines 4-1 exhaust.
                            1985 GS1150ES stock with 85 Red E bodywork.

                            Comment


                              #15
                              I'll make sure the airbox is sealed next time I work on it. It does have the rubber seals. I think I'll use some weatherstripping on the inside of the chrome covers.

                              I will keep the washers in mind. What I don't understand is why I would need to do this when it was new and stock it didn't need it from the factory. Now it is just old and stock but needs it?

                              Is there any documents on the site that show how to test the ignition? New at this but will try anything once!


                              Thank you for all the replies so far! Keep them coming.

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